用户名: 密码: 验证码:
AMAO(多级AO)工艺在污水厂扩建工程中的应用及运行
详细信息    查看全文 | 推荐本文 |
  • 英文篇名:Application and Operation of AMAO Technology (Multi-stage AO) for Expansion Project of Wastewater Treatment Plant
  • 作者:贾建伟 ; 党晓宏 ; 李建洋 ; 杨坤
  • 英文作者:JIA Jian-wei;DANG Xiao-hong;LI Jian-yang;YANG Kun;CSCEC AECOM Consultants Co.Ltd.;
  • 关键词:扩建工程 ; AMAO工艺 ; 工程设计
  • 英文关键词:expansion project;;anaerobic multi-stage anoxic-oxic technology;;engineering design
  • 中文刊名:GSPS
  • 英文刊名:China Water & Wastewater
  • 机构:中国市政工程西北设计研究院有限公司;
  • 出版日期:2019-02-17
  • 出版单位:中国给水排水
  • 年:2019
  • 期:v.35;No.480
  • 语种:中文;
  • 页:GSPS201904017
  • 页数:4
  • CN:04
  • ISSN:12-1073/TU
  • 分类号:76-79
摘要
西安市某污水处理厂二期扩建工程设计规模为2. 5×10~4m~3/d,采用AMAO(多级AO)+高效沉淀池工艺,出水水质执行一级A排放标准。AMAO工艺生物池MLSS可达5 100mg/L,远高于常规AAO工艺(MLSS通常按4 000 mg/L设计),生物池容积可减小20%;无需外加碳源,能优先利用污水中的碳源进行反硝化,省去了常规AAO工艺的混合液回流,脱氮效率大于75%,电耗可降低0. 015 kW·h/m~3。高效沉淀池斜管上升流速设计取低值(11. 37 m/h),省去了后续过滤单元,节约水头约8 kPa,出水SS稳定小于10 mg/L。该工程实际出水水质优于一级A排放标准,部分指标已达到地表水Ⅳ类水质标准,直接运行费用仅为0. 59元/m~3。
        The design treatment capacity of the second phase expansion project of a wastewater treatment plant in Xi'an was 2. 5 × 10~4 m~3/d. The combination process of AMAO( multi-stage AO) and high-efficiency sedimentation tank was adopted to ensure that the effluent quality could reach the first class A discharge standard. The MLSS of the bio-tank could reach 5 100 mg/L,much higher than that of the conventional AAO process( MLSS was usually designed at 4 000 mg/L),so the bio-tank volume could be reduced by 20%. No additional carbon source was needed,and the carbon source in the wastewater could be preferentially used for denitrification, eliminating the mixed liquid reflux in conventional AAO process. The denitrification efficiency of the process was more than 75%,and the power consumption could be reduced 0. 015 kW·h/m~3. The upward-flow velocity of inclined pipe in high-efficiency sedimentation tank was designed at low value( 11. 37 m/h),and the subsequent filtration unit was omitted. The water head was saved about 0. 8 m,and the SS of effluent was stably below 10 mg/L. The actual effluent quality was better than the first class A discharge standard,and some indicators had reached class Ⅳ quality standard for surface water. The direct operation cost was only0. 59 yuan/m~3.
引文
[1]董洋,汪德金,余波.多级AO工艺用于全地下式北京碧水污水处理厂升级改造[J].中国给水排水,2018,34(2):59-62.Dong Yang,Wang Dejin,Yu Bo. Application of multistage AO process in the upgrading and reforming project in underground Beijing Bishui Wastewater Treatment Plant[J]. China Water&Wastewater,2018,34(2):59-62(in Chinese).
    [2]李伟,卢东昱,陈永玲,等.北京市某污水厂基于准地表Ⅲ类水体出水标准的工程实践[J].中国给水排水,2017,33(2):56-60.Li Wei,Lu Dongyu,Chen Yongling,et al. Engineering practice of a WWTP in Beijing City based on quasi-classⅢcriteria of surface water[J]. China Water&Wastewater,2017,33(2):56-60(in Chinese).

© 2004-2018 中国地质图书馆版权所有 京ICP备05064691号 京公网安备11010802017129号

地址:北京市海淀区学院路29号 邮编:100083

电话:办公室:(+86 10)66554848;文献借阅、咨询服务、科技查新:66554700